Painted
- Details
- Parent Category: MG Diary
- Created on 17 May 2013
- Last Updated on 20 May 2013
- Published on 17 May 2013
- Hits: 17
So.. during the last few months I've slowly been building up the engine bay. After much measuring and checking of radiator dimensions I've plumped for a dinky unit from a Suzuki Swift. It is mounted on a custom frame and is angled backwards to ensure that it clears the bonnet. It isn't the thickest radiator so I'm going to ensure that an oil cooler is hooked up using the original take off points that are on the 4AGE engine when mounted in a MR2.
Next up was the inlet manifold,and this was bolted to the head. I acquired a set of 4AGE 20V throttle bodies and set about separating them from their inlet manifold and loosely bolted them to the manifold. As I didn't have a connector for the Toyota throttle pot I took the harder route and knocked up a fixing plate and a threaded adapter to fit the D shaped throttle pot from a Ford/Rover.
I was about to start making the engine loom and discovered that the injectors had an unusual connector. I soon gave up looking for suitable connectors and instead dug out a fuel rail that had some Denso injectors that took mini power timer connectors. Spending a few minutes a night in the shed resulted a week later in a loom for the engine bay. The ECU is an old DTA E48 chose mainly because it was cheap.
Having assembled this much it was time to pull everything out of the engine bay and get ready for a bit of painting. A lot of the junk from the shed was relocated into the garden shed and painting begun. A 2K etch primer was applied to the bare metal and this was followed a few days later with a high build primer then a few coats of an Old English white sort of colour. This is the colour that looks like Tesco Value Custard under fluorescent lighting but thankfully looks better in daylight.
Feb 2013
- Details
- Parent Category: MG Diary
- Created on 04 March 2013
- Last Updated on 08 March 2013
- Published on 04 March 2013
- Hits: 82
After fitting the suspension the brakes were the next job. Last time I made some brake lines i was with copper pipe but this time I decided to use cunifer pipe. This was when I found out how bad the basic Laser brake flaring tool was. Fortunately I manged to lose the forming "top hat" so had to rummage through the tool box and found the old Motaproducts tool donated by my father-in-law a few years ago. It turned out to be a cracking tool and made lovely flares. I later discovered that the line down the transmission tunnel needs to be a bit higher at the front so that the gearbox doesn't touch it when being fitted.

Once the brake lines were fitted the engine and gearbox could go back in. Once installed the next task on the virtual list was to fabricate a bracket for the alternator. It was made from 5mm plate and shared the 2 front mounting holes with the engine mount. Alignment was done with the Mk 1 Eyeball but after assembly it looks like that this needs recalibrating. That plus a bit of play in the alternator mounting hole resulted in 4.5mm misalignment. The alternator mounting hole was drilled out to 12mm and lined with some 12mm OD alloy 1mm thick tube that was a nice fit to the 10mm bolt. A bit of a tweak on the bracket mounting holes resulted in a near perfect alignment. The tension arm came from the pot of odds that one accumulates and will be shortened at some point.

The steering rack and column were fitted to check space etc. Next up is the cooling and fuel injection.
Winter months
- Details
- Parent Category: MG Diary
- Created on 05 December 2012
- Last Updated on 15 February 2013
- Published on 07 January 2013
- Hits: 91
The cold weather put a stop to finishing the spraying so early December I had to find something else to work on. The back axle & spring assembly had been stored under cover beside the shed so this was moved into the dry for some attention.
I will be so glad when all the cleaning of greasy and rusty parts is over and the axle was a mess. Here's the axle before I started.

The spring mounting pads were seized.

The axle was completely stripped down. The front metalastic bushes were drilled out and everything was cleaned with a wire wheel and rust treated then coated with some chassis black.
The diff was rough to turn so was stripped and needed a new pinion oil seal and the pinion front bearing was worn. At this point the list of parts required was growing.
Attention turned to the front suspension and more stripping, removing of grease and rust was undertaken. The kingpins were removed and it then became apparent that the lower bearing surface was corroded and the kingpins were a loose fit into the stub axle.

Attempting to remove the kingpins from the wishbones revealed the next issue. The fulcrum pins were seized to the kingpins and the trunion had a lot of play in the threads. Cue more expense, this time for a set of wishbones. However rather than pay £60 each for standard pattern parts I took what I hope is the better route and purchased a pair of Barry KIng premium wishbones - see http://www.spridgetwishbone.co.uk for more details.

Among the pile of spares I'd been acquiring was a pair of new king pins and fitting. The new king pins were tried in the uprights had the lower bushes were shot. The old ones were drifted out and new ones drifted in and then reamed using a reamer I'd purchased over a year ago. It would have been as cheap to buy refurbished ones but I wanted the challenge and I'm rather enjoying all this.
As you work though these tasks you find that more parts are worn or broken so more parts have been ordered. Even things like 3/8" UNF bolts had to be ordered because I didn't realise I'd need so many. I was thinking of replacing UNF bolts with metric ones but the number of captive nuts and studs would have cause confusion so I'm sticking with the UNF bolts where originally fitted and will use the metric ones on the engine.
As of January 24th the axle, diff and spring assembly has been bolted to the chassis. The handbrake linkages were worn so the holes were welded up and then re-drilled and all painted etc to look good.
With the axle fitted attention was turned back to the front and it was assembled and included poly bushes as well. The original dampers have been retained for now but will probably be modified once the car is on the road. I want to experience the improvements with each change rather than just throw them all on now plus if I did that I'd never finish it.

This is the nearside fitted and just the offside to go. I've also been working on the pedal box and made up some 1/4" spacers to space the clutch and brake cylinders away from the housing. The effect of this is to move the pedals just over an inch towards the bulkhead. Apparently there is still enough pedal travel if you do this.....time will tell if this is the case but being close on 6'2" I need as much space as possible.

Here's the suspension bolted in and the pedal box was about to be assembled and fitted.
Next step will be to plumb in the brake lines then drop in the engine.
Primed for a boost
- Details
- Parent Category: MG Diary
- Created on 09 October 2012
- Last Updated on 07 January 2013
- Published on 09 October 2012
- Hits: 185
Progress seems very slow so I needed something to give me a boost. The rear end has had a lot of attention and a kilo of filler of which most appeared to be sanded off again. The photo below is from part way through the filling stage and I've come on a bit since then. It just needs final sanding and defect filling then will be ready for a primer.

The scuttle and A pillars were next for attention and to ensure that all was aligning correctly the wings and nose were trial fitted. Suddenly it looked like a car again.

The nose section required a bit of welding and took a few evenings to clean to bare metal and was the most awkward item to work on so far. I just couldn't get it to stay still or in a position that I could comfortably work on it, hence 2 evenings work.
To give me that boost and to clear some workshop space I decided to spray the front end. This will then allow me to drop the engine back in and move the hoist out of the shop into another shed. Here's how it looks tonight.

A 4AGE in the hole
- Details
- Parent Category: MG Diary
- Created on 20 July 2012
- Last Updated on 16 October 2012
- Published on 20 July 2012
- Hits: 264
Used up another days leave and made a bit more progress in the engine bay. The usual practice is to fix the engine mounts to the chassis rails on the Konversions after strengthening them. The original engine is mounted on to the suspension turrets with brackets taken from the front of the engine and after a while just sitting and looking at the engine bay that is the route I decided to take.
Hunting through the pile of metals produced some 5mm plate and in another drawer was a Fiesta Mk1 engine mount left over from a Westfield. The Fiesta mounts were ideal for this conversion because it was easy to fit them on the surface from where the original mounts were removed. I know it doesn't seem much complete for a day spent in the garage but I'm chuffed.


